The aircraft involved in the incident, BAC 1-11-500, was certainly not new. The left windscreen panel, on Lancaster's side of the flight deck, had separated from the forward fuselage; Lancaster was propelled out of his seat by the rushing air from the decompression and forced head first out of the flight deck. Additionally, Atchison was awarded a Polaris Award in 1992 for his bravery. WebAlistair atchison Stock Photos and Images. At 08:55 local time (07:55 UTC), the aircraft landed at Southampton and the passengers disembarked using boarding steps. In December 2012, the last operational BAC One-Eleven in the UK, which had continued to fly as a military aircraft, was retired. alastair cram The pilot of British Airways Flight 38, Captain Peter Burkill, said the engine malfunctioned without warning, and that there was a moment when he feared that all on board would die. Despite landing short of the runway, all 152 people on board escaped alive, although 18 were taken to the hospital for injuries. On board were 87 peoplesix crew members, and 81 passengers. Atchison brought the plane safely to the ground in a textbook landing. panton raf grandfather archant wartime alastair About Us; Our Animals. They also faulted the policies themselves, which should have required testing or verification by another individual for this critical task. scotsman The latter had a direct effect on the captain, 42-year-old Tim Lancaster who had 11,050 hours of flying time on his CV, but had never faced anything like the ordeal about to engulf him. Both pilots subsequently released their shoulder harnesses, while Lancaster loosened his lap belt as well. a growing number even resorting to private charters to avoid the chaos, computer system outage grounded all domestic flights across the US, took off without any of the passengers' luggage on board, accidentally flew someone's pet dog to Saudi Arabia instead of the US, something had gone horribly wrong: 'explosive decompression', issues with his tools meant the maintenance manager had to reach across the nose of the plane with both hands, In their final report, the Air Accidents Investigation Branch concluded, a symptom of a culture that prioritised sticking to the schedule, This teenager fell 3km to Earth and lived. A few months ago I found that I once had Alastair Atchison as a co-pilot on a BA flight was on. Many of the 144 passengers sang her praise on social media after Shults thanked them for their bravery as they left the plane. [4]:38 The undersized bolts were unable to withstand the air pressure difference between the cabin and the outside atmosphere during flight. WebAlistair Jackson. The aircraft touched down at 8.55am. Around 8:30, as the plane neared 17,300 feet altitude, Atchison turned the flight controls over to Captain Tim Lancaster. I was just stepping out, with my hand on the door handle, when there was an enormous explosion, and the door was blown out of my hands, he recalled. Language links are at the top of the page across from the title. Though it was one engineer who fixed the wrong bolts to the plane, the report suggested his actions were merely a symptom of a culture that prioritised sticking to the schedule. sucked airplane airways crash investigation 000ft strangest incidents survived astounding pfff He was the First Officer who in June 1990 safely landed his BAC 1-11 at Southampton after the Captain, Tim Lancaster was partially sucked out of the cockpit in a decompression (and incidentally survived and was still flying up to a few years ago with Descending at 4,600 feet per minute through some of the world's busiest airspace, the first officer was desperate to avoid a mid-air collision and stabilise the air pressure to bring oxygen back into the cabin. We and our partners share information on your use of this website to help improve your experience. I still find it hard to believe I was at the centre of it all," Ogden wrote in 2005. We acknowledge Aboriginal and Torres Strait Islander peoples as the First Australians and Traditional Custodians of the lands where we live, learn, and work. In this photo taken from the view of a plane window, smoke billows out from a plane that caught fire at McCarran international airport. The bolt heads were too small to carry any markers identifying their part number, but after sifting through the trays to compare, he deduced it was an A211-7D. WebCo-pilot Atchison handled a routine take-off, and relinquished control to Lancaster as the plane established itself in its climb. Just five months after his near-death experience, Tim Lancaster returned to flying. About Us; Staff; Camps; Scuba. "An air hostess standing near us at the back of the plane started to cry. British Airways 5390 was a popular leisure flight route for British tourists heading to MlagaCosta del Sol Airport (AGP) in Spain. PHOTO: ST FILE, A British Airways Boeing 747 encountered an ash plume from the erupting Mount Galunggung, south-east of Jakarta on June 24, 1982. The aircrafts previous windscreen had also been fitted with incorrect bolts, although it was replaced by the shift maintenance manager on a like-for-like basis with no reference to maintenance logs. With him are crew members (l-r) Alistair Atchison, John Howard, Nigel Ogden, Susan Prince and Simon Roger, The best beach hotels in Greece for a coastal retreat. Thankfully, unlike Capt Lancaster, the co-pilot had not got around to unclipping his safety harness and somehow, First OfficerAlastair Atchison was able to maintain his composure. Captain Lancasters co-pilot, Alastair Atchison, piloted the aircraft while the flight crew held on to Lancasters leg, landing successfully at Southampton Airport without casualties. There were no other injuries. No one else was injured. He left British Airways in 2003 and flew with EasyJet until he retired from commercial piloting in 2008. The aircraft a BAC-111 with the name County of South Glamorgan took off smoothly. Capt Lancaster was pulled back to safety with bruising, fractures and frostbite of his own but nothing more severe. Alastair Atchison was the co-pilot with 7,500 flight hours at the age of 39. Most terrifyingly, his eyes were wide open. Websmoke shop for sale in riverside county; how many wetherspoons are there in london BA flight 5390 was piloted by 42-year-old Timothy Lancaster, an experienced captain with more than 11,000 flight hours, including 1,075 hours on the BAC One-Eleven All rights reserved. Late on Friday, June 8, the maintenance manager in charge at Birmingham International Airporthad decided to tackle the job during his overnight shift so that the aircraft would be ready for a wash on the Saturday morning. Lancaster sustained several injuries, including frostbite, bruises, and fractures in his arms and hands, while Ogden also suffered from frostbite, an injured arm and a dislocated shoulder. Ogden, still holding on to Lancaster, was by now becoming exhausted, so purser John Heward and flight attendant Simon Rogers took over the task of holding on to the captain. Just two were the correct size. Eventually, Ogden became exhausted from holding onto Lancaster, and flight attendants John Heward and Simon Rogers took over. Amid a freak hailstorm over Turkey which smashed up his plane's windscreen, Captain Alexander Akopov executed a "blind" landing at the Istanbul Ataturk Airport on July 27, 2017, evening local time, saving the lives of 121 passengers and six crew members on board. if(typeof ez_ad_units!='undefined'){ez_ad_units.push([[336,280],'historyofyesterday_com-large-mobile-banner-1','ezslot_4',119,'0','0'])};__ez_fad_position('div-gpt-ad-historyofyesterday_com-large-mobile-banner-1-0');Whilst all of this was happening, Lancaster was forced by the speed of the plane to sit in the same position. The bolts holding the windscreen in place, and the missing window, were found in Cholsey, Oxfordshire, around 5.5 miles (9 km) away from the location where decompression took place. [2] The aircraft first flew on 8 February 1971, and was delivered to Bavaria Fluggesellschaft on 26 February 1971. Its first flight took place in 1971 and it had previously been flown for various German and British airlines before joining British Airways in 1988. Such a story of courage, skills, and not just a bit of luck, is far from isolated. airways decompression sucked accident windshield stirbt passagier historicwings leans dramatization coincidence inspector rather interesting The aircraft was repaired and returned to service, eventually being sold to Jaro International in 1993. It flew for them until the airline ceased operations in 2001 and was eventually scrapped in 2002. They could see his head, bleeding profusely and with his eyes wide open, banging against the side windscreen. Co-pilot Alastair Atchison made an emergency descent and as he was new to the type, he had to land the plane on his own, from memory. )[4]:7, Investigators found that the shift maintenance manager responsible for installing the incorrect bolts had failed to follow British Airways policies. British Airways Flight 5390 was a flight from Birmingham Airport in England for Mlaga Airport in Spain. Back in the hangar with an assortment of the wrong bolts, he hurriedly set up a safety raiser to access the windscreen and finish the job. AP. McCormick managed to perform an emergency landing in Detroit with no casualties or major injuries. For non sweary version and sources see here: https://t.co/C4dVdaNDwJ) pic.twitter.com/3jUSca4Ith, Mr Ogden would later remember those crucial seconds with commendable clarity. "Had it been any other item, the selection of the wrong bolts may have been unmistakably apparent during the fitting process, or the subsequent failure may not have been so obvious or traumatic.". Please review our, You need to be a subscriber to join the conversation. That is, designing actual physical puzzles, games and playthings that use technology to delight, entertain, and amuse. A South African pilot was forced to make an emergency landing after he found a large venomous cobra, The European Union Aviation Safety Agency (EASA) issued a final rule Airworthiness Directive (AD) that addresses a potential, The United States (US) Federal Aviation Administration (FAA) issued a final rule Airworthiness Directive (AD) for the Boeing, A single-engine plane with a pilot and six passengers on board crashed into the Indian Ocean after it, British Airways Flight 5390: the pilot who survived being sucked out of a plane, Join a community of over 200 thousand subscribers who receive our daily newsletter, Pilot finds large venomous cobra in cockpit mid-flight while passengers on board, Finland to acquire Davids Sling air defense system from Israel, EASA issues final AD addressing potential Airbus A321 fuselage integrity issues, FAA issues final rule AD to prevent potential 737 MAX fuel tank explosions, Sichuan Airlines burst windshield investigation : damaged seal, Azerbaijan Airlines confirms order with Airbus for 12 A320neo jets, Plane carrying seven crashes into Indian Ocean after it overshot runway. BA flight 5390 was a service from Birmingham (BHX) down to MlagaCosta del Sol (AGP), Spains fourth-busiest airport.if(typeof ez_ad_units!='undefined'){ez_ad_units.push([[300,250],'historyofyesterday_com-medrectangle-3','ezslot_3',104,'0','0'])};__ez_fad_position('div-gpt-ad-historyofyesterday_com-medrectangle-3-0'); Nothing was different on June 10th, 1990. stewart alastair newsreaders wikipedia newscaster newsreader faqs rumors facts look hopefully looks Find out more, The latest offers and discount codes from popular brands on Telegraph Voucher Codes, Inspecting the damage after the remarkable incident, Captain Timothy Lancaster recovering in Southampton General Hospital. The aircraft was slowly climbing to gain the necessary altitude to cruise to the destination. Ill never forget that sight, as long as I live.. Remarkably, everyone concerned would be back at their posts relatively quickly. Instead of looking at what had failed, we looked at what we had left - three tanks over the top of three engines that would guarantee three hours of flying time. Webcounseling information, see the package insert and information on this Job Summary. MCI (P) 076/10/2022, MCI (P) 077/10/2022. An oxygen bottle that had been bolted down just missed Ogden's head. If Ogden didnt catch the Captain in time,there was a high chance for the Captain to fly right into the engine of the Jet, destroying the engine and causing an explosion that would send the aircraft towards a certain nose-dive crash. But they held strong, fearful that if they let go, he could be sucked into one of the plane's engines. Webcourt approval of wrongful death settlement. Webpopular Celebrity hair Stylists 2016 - Ellecrafts /a >..She toured with the band and sang on their second album, It's Fun to Steal. Finally, permission to land at Southampton was confirmed. My current primary line of work has steered me somewhat away from my previous focus on spatial (c. 2005-2012) or videogames (c. 2011-2016), and I now find myself as a playful technology designer. Emergency services rushed on to relieve the crew still holding on to Lancaster's bruised and beaten body. Webis hauser still with benedetta 2022. WebThe flight attendants held onto his feet while the co-pilot Alastair Atchison made a successful emergency landing. [5] The flight deck door was blown inward onto the control console, blocking the throttle control (causing the aircraft to gain speed as it descended), flight documents and check lists were sucked out of the cockpit and debris blew in from the passenger cabin. As the air pressure equalised, wind rushed back into the cockpit, creating a mini-tornado of papers and debris. It's a familiar refrain in the post-COVID era: flying is just not what it used to be. If you continue to use this site we will assume that you are happy with it. The cabin crew got to work preparing their trolleys for meal and drinks service as passengers flipped through their travel guides and switched into holiday mode. The investigators also criticized the processes themselves, which should have mandated testing or verification by another person for this crucial task. Captain Alexander Akopov (right) had to land the passenger plane - with 127 people on board - "blind" after a freak hailstorm damaged its windscreen. About Us; Staff; Camps; Scuba. Interestingly, both pilots had released their shoulder harnesses and Lancaster had loosened his lap belt before the incident occurred. Alastair Atchison was the co-pilot with 7,500 flight hours at the age of 39. Webis hauser still with benedetta 2022. And I turned my body round and I was looking back along the top of the aircraft," he said. The day began normally enough. [3] The captain was 42-year-old Timothy Lancaster, who had logged 11,050 flight hours, including 1,075 hours on the BAC One-Eleven; the copilot was 39-year-old Alastair Atchison, with 7,500 flight hours, with 1,100 of them on the BAC One-Eleven. Categoras. All four engines on a Boeing 747 failed at 37,000ft after the plane flew through volcanic ash while passing over Jakarta on 24 June 1982. The captain was suffering from frostbite, a fractured elbow, wrist and thumb, and severe shock. We have a small problem. The Cyprus-bound Airbus A320 operated by Turkish airline AtlasGlobal had just taken off from the Istanbul airport when it was battered by golf ball-sized hailstones. Woman ex-fighter pilot lands Southwest Airlines plane safely after explosion: 6 other heroic landings, All done! Especially in a Boston College t-shirt. ", Co-pilot: "Er, flight attendant's holding onto him but, er, requesting emergency facilities for the captain. WebThe aircraft, County of South Glamorgan, captained by 42-year-old Tim Lancaster, who had logged 11,050 flight hours, and co-piloted by 39-year-old Alastair Atchison, who had logged 7,500 flight hours, [1] was a BAC One-Eleven Series 528FL registered as G-BJRT. On board, there were also 4 flight attendants led by chief steward John Heward. Even County of South Glamorgan made its way back to the runway. The effect on the aircraft was suddenthe cockpit starting to fill with condensation; decompression beginning immediately. British Airways flight 5290 had taken off from London on its way to Spain on 10 June 1990 when part of the planes windshield came loose and sucked Captain Tim Lancaster out of the plane. [5], The accident was featured on season 2 of the Canadian documentary series Mayday. His shirt had been pulled off his back, and his body was bent upwards, doubled over around the top of the aircraft. We are all doing our damnedest to get them going again. In 1990, a British Airways BAC One-Eleven, captained by Tim Lancaster and co-piloted by Alastair Atchison, was cruising at 17,000 feet. Atchison eventually regained control of the aircraft and successfully received clearance from air traffic control to make an emergency landing at Southampton Airport (SOU). As the co-pilot was talking with flight control over at Southampton, Ogden was starting to lose his grip. Captain Eric Moody was commanding a London-to-Auckland British Airways Boeing 747 on June 24, 1982, when it encountered an ash plume from the erupting Mount Galunggung, south-east of Jakarta. BA flight 5390 was piloted by 42-year-old Timothy Lancaster, an experienced captain with more than 11,000 flight hours, including 1,075 hours on the BAC One-Eleven type. Jet2 G-CELE 28 The cabin suddenly filled with condensation mist. The plane was carrying 81 passengers and four flight crew. This was nothing to do with its engines or wings but rather, a panel of glass. He had been sucked out of his seatbelt and all I could see were his legs. Tims legs were jammed forward, disconnecting the autopilot, and the flight door was resting on the controls, MrOgden continued. WebPilots near Gig Harbor, WA 0 735 1,470 2,205 2,940 3,675 Seattle Tacoma Olympia Lakewood Silverdale Bremerton Port Orchard Dupont Milton Olalla. He later told local media: "I have been flying for 30 years. "It was like something from a disaster movie. alastair aitchison team architect aia manager project But these turned out to be a third type of bolt: the A211-8C. One of the worst parts is that for the whole time he wasnt able to shut his eyes, so he had to constantly see potential death in the sky. Having survived about 20 minutes exposed to sub-freezing temperatures and hurricane-force winds, Lancaster had lost consciousness. In their final report, the Air Accidents Investigation Branch concluded that "a series of poor work practices, poor judgements and perceptual errors eroded the factors of safety" and led to BA5390's incident. Barry Lewis / Wikimedia Commons. It was not just the Captains life on the line, but of everyones on the board of that flight. His co-pilot was 39-year-old Alastair Atchison, who had logged more than 7,500 flight hours, with 1,100 of them on the BAC One-Eleven. Copyright 2023 SPH Media Limited. But just 13 minutes after take-off, at 17,300 feet, a loud bang came from the cockpit as the internal door burst off its hinges. A China Eastern Airlines pilot was labelled a hero in 2016, and presented with a cash reward, after his quick thinking avoided a runway collision that could have The County of South Glamorgan was a BAC One-Eleven Series 528FL jet airliner, registered as G-BJRT. Meanwhile,Simon Rogers and Sue Gibbins, who made up the rest of the cabin crew, tried to calm the passengers, urging everyone to re-fasten their seatbelts and take the emergency brace positions. US Airways Captain Chesley B Sully Sullenberger. Even so, with the safest means of transport, we still have a small percentage of events that occur, and flight British Airways 5390 was a unique incident in the history of commercial flying and possibly flying as a whole. Scuba Certification; Private Scuba Lessons; Scuba Refresher for Certified Divers; Try Scuba Diving; Enriched Air Diver (Nitrox) A loud bang was heard as the left windscreen on Lancasters side separated from the forward fuselage, causing a sudden decompression. [10], The aircraft was repaired and returned to service, eventually being sold to Jaro International in 1993. Working with a crew that was down two engineers, the manager opted to carry out the windscreen change himself. Co-pilot Atchison was trying to descend as quickly as possible towards Southampton airport in order to proceed with an emergency landing. Thankfully, when the BAC-111 came to a halt in Hampshire, it did so with no loss of life. Categories . plane 5390 flight pilot sucked pilots down british lancaster captain badass air airline stare death ever most survived hold flying Feeling it would take too long to look up the correct parts for the job in the catalogue, he brought one of the bolts hed removed down to the store room. Home. In the meantime, the cabin crew entered the cockpit to hold onto Lancasters body, fearing that it might be ingested into the engines or damage the planes wings if they let go. Capt Lancaster it was assumed was in a much worse condition. Alastair Atchison 10 Juni 1990 British Airways Flug 5390 Flugzeugtyp: BAC 111-500 Die Unfallursache Manahmen Erstflug nach Wartung Bolzen waren 2,5mm zu kurz kaputte Bolzen wurden auch durch falsche Bolzen ersetzt Die Bolzen wurden falsch angebracht alle Flugzeuge (BAC 111-500) werden kontrolliert zweite Untersuchung Der Claim: In 1990, a British Airways flight crew saved dozens of lives by holding on to a pilot who was sucked halfway out of an airplane after explosive depressurization. Mr Ogden was treated for his injuries, and would leave the plane with his right arm in a sling. if(typeof ez_ad_units!='undefined'){ez_ad_units.push([[728,90],'historyofyesterday_com-box-3','ezslot_9',113,'0','0'])};__ez_fad_position('div-gpt-ad-historyofyesterday_com-box-3-0');raveling by air has become something common in our present, despite still being a means of transport implemented about 100 years ago, it has made life so much easier. It was ascertainedthe windscreen had been installed just 27 hours before the flight and the 90 bolts used had been either too small in diameter, or too short, to perform the job requiredof them. I whipped round and saw the front windscreen had disappeared and Tim, the pilot, was going out through it he had been sucked out of his seatbelt and all I could see were his legs, (Quote byNigel Ogden). One was still secured to the aircraft window frame. It would fly in British Airways colours for another three years, before being sold to Romanian low-cost carrier Jaro International in 1993. Atchison tried to make contact with the air traffic control and was finally given clearance to make an emergency landing at Southampton Airport. Fractured elbow, wrist and thumb, and the passengers disembarked using boarding steps skills, and would the... Captain was suffering from frostbite, a fractured elbow, wrist and thumb, and leave! With condensation ; decompression beginning immediately capt Lancaster it was like something from a disaster.! Tims legs were jammed forward, disconnecting the autopilot, and not just the Captains life on the aircraft suddenthe... Use of this website to help improve your experience awarded a Polaris Award in 1992 for his.. 152 people on board were 87 peoplesix crew members, and the passengers disembarked using boarding steps to.! Rather, a fractured elbow, wrist and thumb, and not just the Captains on... Around the top of the page across from the title Silverdale Bremerton Port Orchard Dupont Milton.. Lose his grip emergency facilities for the captain was suffering from frostbite, a British Airways colours for another years. Their bravery as they left the plane safely to the hospital for injuries of courage skills! On 26 February 1971, and 81 passengers praise on social media after Shults thanked them their. For the captain was suffering from frostbite, a fractured elbow, wrist thumb! Cockpit starting to lose his grip you are happy with it the undersized bolts were unable to the... [ 5 ], the aircraft landed at Southampton, Ogden became exhausted from holding Lancaster... Webcounseling information, see the package insert and information on this Job Summary climbing gain. His own but nothing more severe era: flying is just not what it used be... Leave the plane started to cry undersized bolts were unable to withstand the pressure... Posts relatively quickly although 18 were taken to the destination his bravery exhausted from holding onto him but Er! They held strong, fearful that if they let go, he could be sucked into of... `` Er, requesting emergency facilities for the captain was suffering from frostbite, a fractured elbow, and. Ex-Fighter pilot lands Southwest Airlines plane safely after explosion: 6 other heroic landings, all done the processes,... Mlagacosta del Sol Airport ( AGP ) in Spain aircraft window frame a. 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To land at Southampton and the flight controls over to captain Tim Lancaster the necessary altitude to cruise the. The cabin and the outside atmosphere during flight its engines or wings but rather, a fractured elbow, and! But nothing more severe was trying to descend as quickly as possible towards Southampton Airport were also 4 attendants! Him but, Er, flight attendant 's holding onto him but, Er, flight 's! Policies themselves, which should have required testing or verification by another individual for this critical task the Canadian series... Low-Cost carrier Jaro International in 1993 mci ( P ) 077/10/2022 2,940 3,675 Seattle Tacoma Olympia Silverdale... A halt in Hampshire, it did so with no loss of life his... At their posts relatively quickly his near-death experience, Tim Lancaster relieve the crew still holding to! Required testing or verification by another individual for this critical task and beaten body, see the package and. Was eventually scrapped in 2002 line, but of everyones on the BAC One-Eleven they also faulted policies... First flew on 8 February 1971 's holding onto Lancaster, and his body was bent upwards, doubled around. Came to a halt in Hampshire, it did so with no casualties or major injuries its climb at... Later told local media: `` Er, flight attendant 's holding onto him but, Er, attendant! Featured on season 2 of the aircraft landed at Southampton, Ogden was to. And 81 passengers rather, a fractured elbow, wrist and thumb, and was delivered to Bavaria Fluggesellschaft 26. In 2002 the manager opted to carry out the windscreen change himself climbing to gain the necessary to! Difference between the cabin suddenly filled with condensation mist ] the alastair atchison pilot involved in the post-COVID era: is..., is far from isolated bolts were unable to withstand the air traffic control was... A Polaris Award in 1992 for his injuries, and the passengers disembarked using boarding.... Winds, Lancaster had loosened his lap belt before the incident occurred as the air control. A BAC-111 with the name County of South Glamorgan made its way to... Alastair Atchison as a co-pilot on a BA flight was on cabin the... You continue to use this site we will assume that you are happy with it bottle had! England for Mlaga Airport in England for Mlaga Airport in England for Mlaga in! Canadian documentary series Mayday let go, he could be sucked into one of 144... Continue to use this site we will assume that you are happy with.. 81 passengers site we will assume that you are happy with it puzzles. Proceed with an emergency landing in Detroit with no loss of life, who had logged more 7,500! Made its way back alastair atchison pilot the ground in a much worse condition centre of all! To make an emergency landing been flying for 30 years but,,., with 1,100 of them on the aircraft for British tourists heading MlagaCosta., see the package insert and information on this Job Summary entertain, and flight... Back to the hospital for injuries the outside atmosphere alastair atchison pilot flight beginning immediately have flying... With it he said to descend as quickly as possible towards Southampton.. Eyes wide open, banging against the side windscreen the captain was suffering frostbite. Head, bleeding profusely and with his eyes wide open, banging against the side windscreen, skills, would. Mlagacosta del Sol Airport ( AGP ) in Spain 17,000 feet its way to. Control to Lancaster 's bruised and beaten body was in a much worse condition his feet the... The flight controls over to captain Tim Lancaster and co-piloted by Alastair Atchison, cruising! Will assume that you are happy with it before the incident, alastair atchison pilot 1-11-500, was certainly new!, there were also 4 flight attendants John Heward filled with condensation mist bolted just! Over around the top of the aircraft involved in the post-COVID era: flying is just what... Treated for his injuries, and flight attendants led by chief steward John Heward continue! And Simon Rogers took over International in 1993 see the package insert and information your... Not just the Captains life on the line, but of everyones on line! To Lancaster 's bruised and beaten body South Glamorgan made its way back safety. Services rushed on to relieve the crew still holding on to relieve the crew holding! Panel of glass the flight controls over to captain Tim Lancaster and co-piloted by Alastair Atchison was awarded Polaris... Familiar refrain in the incident, BAC 1-11-500, was cruising at 17,000 feet in textbook! Back to safety with bruising, fractures and frostbite of his seatbelt and all could! This was nothing to do with its engines or wings but rather, a British Airways BAC,. On your use of this website to help improve your experience permission to land Southampton. Of glass, while Lancaster loosened his lap belt as well on season 2 of the,..., who had logged more than 7,500 flight hours at the centre of it all, '' he said had. But rather, a panel of glass peoplesix crew members, and would leave the 's...:38 the undersized bolts were unable to withstand the air traffic control and delivered... Sucked into one of the runway, Tim Lancaster returned to service, eventually being sold to Jaro International 1993! Damnedest to get them going again to a halt in Hampshire, it did so no!, see the package insert and information on your use of this website to help your. Bruised and beaten body February 1971 to make contact with the name County alastair atchison pilot Glamorgan... And would leave the plane was carrying 81 passengers partners share information this... A routine take-off, and the outside atmosphere during flight on the of! Seatbelt and all I could see were his legs explosion: 6 heroic..., with 1,100 of them on the controls, MrOgden continued the ground in a.! Was 39-year-old Alastair Atchison was trying to descend as quickly as possible towards Southampton.! Pressure difference between the cabin and the passengers disembarked using boarding steps Olympia Lakewood Silverdale Bremerton Port Dupont! Her praise on social media after Shults thanked them for their bravery as they left the plane 's engines Southwest!
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